*CONTINUED*
I got a replacement bottom end and cleaned both surfaces:
Fitted a new Cosworth Headgasket:
Head on:
Timed Up:
New Oil block for Gauge and Turbo Feeds - Cheers Guy! :
And this was how the second turbo setup looked, neat!:
This one ran awesome, until this happened:
So I swapped my Quaife LSD into a P11-144 Gearbox:
The engine was a bit noisy so I checked out a rod bearing and found this:
LUCKY!! The crank was OK so I changed the bearings and it was all good.
I then thought it was now or never to dyno this setup - while it was working!
Unfortunatelty for reasons that we didnt know at the time, after a few abandoned runs on the dyno, it started misfiring so I took it home and put it back in the garage:
Took the engine back out to see what had occurred:
To my horror I found this:
#4 Piston was Melted through.
END OF SETUP 2.